precisionworks
Flashaholic
A 3 hp motor & VFD had been purchased for installation on the mill. After buying the push-pull vise for the drill press, it seemed like that machine would really benefit from a larger motor & variable speed drive. The drill press is a Craftsman, purchased new around 1982, made by the Atlas Press Company - the same company that made the Craftsman metal lathe. I saw one in an Atlas catalog & it had a larger motor & a conventional (wide) belt drive. The first operation is fitting a four step pulley.
The eight step aluminum pulleys gives a speed range from 380-8550 rpm. And the "belt" has barely the ability to transmit 1/2 hp. The front pulley was pulled & the shaft measured:
The shaft is 25mm metric, and a metric bore pulley couldn't be found, so I ordered a 7/8" bore Baldor/Maska four step.
The bore indicated about .0001" total runout using the 3-jaw chuck, so it was ready for boring out. Since the bore needed to be about .109" larger, three passes were made removing .025" each time, followed by .020", followed by .010", then .005". These cuts were made using the dial on the cross slide, which is good enough for roughing work. A dial test indicator was used to get close to the target dimension.
The target dimension was between .9843" and .9845". Any larger than .9845" would give a loose fit, and any smaller than .9843" would make it hard to install the pulley on the shaft. The last pass showed a mic reading of .9842" which was just a bit small, but the pulley was removed from the lathe for trial fitting on the shaft - you can always go back for another cut if needed. Firm blows were able to get the pulley started but it was too tight, even after warming the pulley with a propane torch. Back to the lathe for one more cut, without disturbing the last setting. The 3/4" boring bar will deflect about .0002" when extended 3", so one more pass should remove that amount. The boring bar was run in with power feed, and run back out with power feed. The insert did not touch on the infeed, but just barely made contact as it backed out. The mic showed that the bore was .9844", pretty close to ideal. The pulley was again warmed with the torch & seated nicely. The dial test indicator showed .0002"-.0003" total runout on the bore 😀
The old motor & mount were removed & distance from top of pulley to top of mounting holes measured at 5.75". To make the new motor fit, a piece of 5" wide, 1/4" thick flat stock was welded to the motor base.
The motor plate is marked & ready to drill. More to follow tomorrow.
The eight step aluminum pulleys gives a speed range from 380-8550 rpm. And the "belt" has barely the ability to transmit 1/2 hp. The front pulley was pulled & the shaft measured:
The shaft is 25mm metric, and a metric bore pulley couldn't be found, so I ordered a 7/8" bore Baldor/Maska four step.
The bore indicated about .0001" total runout using the 3-jaw chuck, so it was ready for boring out. Since the bore needed to be about .109" larger, three passes were made removing .025" each time, followed by .020", followed by .010", then .005". These cuts were made using the dial on the cross slide, which is good enough for roughing work. A dial test indicator was used to get close to the target dimension.
The target dimension was between .9843" and .9845". Any larger than .9845" would give a loose fit, and any smaller than .9843" would make it hard to install the pulley on the shaft. The last pass showed a mic reading of .9842" which was just a bit small, but the pulley was removed from the lathe for trial fitting on the shaft - you can always go back for another cut if needed. Firm blows were able to get the pulley started but it was too tight, even after warming the pulley with a propane torch. Back to the lathe for one more cut, without disturbing the last setting. The 3/4" boring bar will deflect about .0002" when extended 3", so one more pass should remove that amount. The boring bar was run in with power feed, and run back out with power feed. The insert did not touch on the infeed, but just barely made contact as it backed out. The mic showed that the bore was .9844", pretty close to ideal. The pulley was again warmed with the torch & seated nicely. The dial test indicator showed .0002"-.0003" total runout on the bore 😀
The old motor & mount were removed & distance from top of pulley to top of mounting holes measured at 5.75". To make the new motor fit, a piece of 5" wide, 1/4" thick flat stock was welded to the motor base.
The motor plate is marked & ready to drill. More to follow tomorrow.
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