Today, I tested several methods to revive a unit suffering from the flex failure. Here's my findings so far:
1. Solder blob to back of PCB idea.
This involves placeing a solder bridge between the ground of the PCB and the housing. It can be done without dismantling the head. The retainer does have to be removed and a new one installed in its place after the service.
I started with 5 bad units and got everyone one of them to work - initially. Mike came in and torqued them all quite hard and made all of them except two fail again.
2. Remove Bezel approach.
With this fix, I removed the bezel and tweaked the insides. This was more effective than the solder fix above but required more work. I tried this on 3 units and got all of them to work 100%, even with battery squashing torque.
First, you have to remove the bezel. Loctite holds it in place so I tried several methods to break the seal. Both involved heating the head up to about 200+ degrees. One method involved placing a soldering iron against the head and the other method involved dropping the head in boiling water like an egg.
About half the units I tried loosened up by the above methods. Some would not budge.
Once the bezel is off, I removed the PCB from the bezel. Next, I ground off the HA around the bezel lip that faces the PCB. A dremel did well on this. I also took some of the HA off the bezel threads as well. Next, I applied blobs of solder around the upper ring of the PCB so it would be sure to make contact with the bezel.
Finally, I reattached the bezels and stressed test the lights by placing the 2AA pack on and turning it as tight as I can. All the units that made it to the bezel step worked 100%.
It is a real bear to get the bezel off though and I am looking for an easier way to fix all these bad units.
More to come..
Peter Gransee