Here goes: my first attempt at something like this...
I had three ProPoly 4AAs, two weren't working. After taking them apart I found the cause. Battery leakage had corroded the two rivets that hold the springs in the bottom of the light and are an integral part of the switching mechanism. The ProPolys are such good battery vampires I failed to realize the obvious: batteries that are being vampired tend to bleed.
Streamlight ProPoly 4AA Switch Cleaning - for lights that work intermitently or stop working and for users that want to fix it themselves and avoid dealing w customer service. Warning - attempting to fix this yourself may cause loss of warranty support.
Tools needed:
Long nose pliers - to turn the plastic nut under the rubber boot if you can't do this using your fingers.
Flat thin object for carefully lifting the plastic retainers - the SAK file was perfect.
Knife blade to begin the switch case separation.
Awl to scrape corrosion off of switch contact rivets.
1. Try to turn the plastic nut under the rubber boot by squeezing tightly as low on the boot as your fingers allow. Turn slowly, you are not fighting the nut thread friction as much as you are the rubber boot friction. You only need about two turns. If you can't get it use pliers...
http://img386.imageshack.us/my.php?image=slppstart1262ze7.jpg
The boot is fairly durable, but obviously needs to be treated with some consideration.
2. Once the switch unit is out use a flat
thin object to carefully lift the retainer and then a thin blade to start to pry open the switch. Get a one mm gap or so, remove the flat thin object from the retainer and do the same procedure on the other side. Once both sides have a small gap, continue to pry apart the two sides, working both sides evenly. Open it while it is sideways for best part placement retention, and in a place where small parts won't get lost.
http://img168.imageshack.us/my.php?image=slppswtchparts1266dj8.jpg
This is what is inside. The metal washer makes contact with both rivets to close the switch. It seems to be made of material that doesn't corrode easily. None of the three I saw needed cleaning. This was my third I took apart and the only one I broke the retaining clip on, which hasn't turned out to be a problem because of the way the switch housing is engineered.
3. The two rivets on the first two lights were very dark from corrosion and needed extensive scraping to clean them. Some deoxit applied after cleaning would be a wise move. After testing the first switch I had to go back and clean the edge of the rivets to establish electrical contact, even though it doesn't look like it would matter.
After reassembly I tested the switch function with a continuity tester.
4. Drop the switch module it into the body. The switch is slightly offset so it must be put in correctly to line up with the hole. Place the batteries in and screw the bezel/light engine on to make the switch stick out firmly. This will aid you when screwing the boot/plastic nut on.