wquiles
Flashaholic
I have been debating checking the pre-load on my PM1236 lathe now that it has been in service for about 18 months or so, but I think that based on what I found today, I am just going to leave it alone for now. And checking the lathe was not my goal today - that was just an accidental result of the work today ...
This all started when I was making heatsinks for the "D" body. Sometimes I make them, sometimes I buy them, but today I wanted to make several of them for use in projects.
I started with a bar of 6061 Al, 1 and 3/8" dia, and the part sticking out of the chuck is close to 9 inches, so I used my Royal live center to keep things steady:
I then cleaned up the OD with my PCD insert and Accu-Lube, spindle speed of about 900 rpm, by hand (no auto feed):
I then proceeded to leave the "lip" in the heatsink, and turn down the body section to close to 1.347" OD. I did a deep cut in between each one to delineate each one. I used the same tool, and did all of them (8 of them) one right after the other, and used the DRO to stop at the same OD for each part:
I then cut them all up in the metal band saw (commercially available heatsink on top for illustration purposes):
Since I have a lip with a slightly larger OD, it is hard to hold in the chuck, so I took a small section of a D mag (I wonder where I can find some scrap pieces .......) and I slightly turned the ID to allow a press fit of these new heatsinks, so that I could then clamp on the "ring" and grab the heatsink inside the ring without having to worry about the chuck damaging the finish. Kind of a poor mans custom collet:
I then press fit each of the heatsinks to clean/true the bottom side - the "collet" worked perfectly:
The thing was that all 8 heatsinks fit pretty well in the "collet" ring, so I though that the OD was probably very close, even though I turned the piece over 9 inches:
So I figured that although I did not try to test the accuracy of the lathe on purpose, this was as a good time as any to check things out. So out came the micrometer ...
And after testing all of them, I found a variation of only 0.00080 over the 9" or so:
So unless I hear otherwise from you guys the real experts (Barry?), I am leaving my lathe as is for now, and will keep using it without worrying about needing to adjust something.
Will
PS
For those wondering, this is the ID of the collet:
And yes, I missed the target OD by about 1 mil too large - I will have to lightly sand those to fit , although of course that is always better (and easier) than adding metal back
This all started when I was making heatsinks for the "D" body. Sometimes I make them, sometimes I buy them, but today I wanted to make several of them for use in projects.
I started with a bar of 6061 Al, 1 and 3/8" dia, and the part sticking out of the chuck is close to 9 inches, so I used my Royal live center to keep things steady:
I then cleaned up the OD with my PCD insert and Accu-Lube, spindle speed of about 900 rpm, by hand (no auto feed):
I then proceeded to leave the "lip" in the heatsink, and turn down the body section to close to 1.347" OD. I did a deep cut in between each one to delineate each one. I used the same tool, and did all of them (8 of them) one right after the other, and used the DRO to stop at the same OD for each part:
I then cut them all up in the metal band saw (commercially available heatsink on top for illustration purposes):
Since I have a lip with a slightly larger OD, it is hard to hold in the chuck, so I took a small section of a D mag (I wonder where I can find some scrap pieces .......) and I slightly turned the ID to allow a press fit of these new heatsinks, so that I could then clamp on the "ring" and grab the heatsink inside the ring without having to worry about the chuck damaging the finish. Kind of a poor mans custom collet:
I then press fit each of the heatsinks to clean/true the bottom side - the "collet" worked perfectly:
The thing was that all 8 heatsinks fit pretty well in the "collet" ring, so I though that the OD was probably very close, even though I turned the piece over 9 inches:
So I figured that although I did not try to test the accuracy of the lathe on purpose, this was as a good time as any to check things out. So out came the micrometer ...
And after testing all of them, I found a variation of only 0.00080 over the 9" or so:
So unless I hear otherwise from you guys the real experts (Barry?), I am leaving my lathe as is for now, and will keep using it without worrying about needing to adjust something.
Will
PS
For those wondering, this is the ID of the collet:
And yes, I missed the target OD by about 1 mil too large - I will have to lightly sand those to fit , although of course that is always better (and easier) than adding metal back
Last edited: